killed pump #1 due to a combination of too much increase of pressure, blocked supply line, and blocked return line on the steering box.
Replaced it and fixed the blocked lines. Left the line pressure stock and threw in half a bottle of lucas too. Seems to be working fine but I think I'm still going to up the pressue, just one washer this time. I can still make the pass. side piss brake fluid if I stand on it. Need to redo the caliper seals and it should be cherry.